11-14-2020, 09:19 AM
(11-14-2020, 07:49 AM)SidekickTripper Wrote: Update:all; looks good.
Vehicle temp ECT sensor verified 180 317 ohms
MAF (Brand Most Plus Part number M3389 102015)
Koeo:
Bl/Blk 12.57 VDC (Battery voltage)
Blk .02 VDC
Gry 1.64 VDC
Running:
1.96 VDC 800 RPM
volts rise with acceleration
ISC 14.2 ohms at operating temp
Pinched fresh air hose dies immediately, starts pinched then idles at approx 500rpm
TPS: .84 volts idle and throttle swing to 4.28 volts
Tech 1
Rich/Lean : Rich
IAC Air Flow: 28 L/Min
IAC Adjust Monitor :0%
Spark Advance: varies 5-12 degress
Injector Pulse width: 4.320
STFT 128
LTFT 128
HO2 903 MV not varying
O2S Activation Activated (Closed loop)
TPS: .84 VOLTS
Throttle Angle: .0 degrees
ECT reads 145F ( verified 180F infraed and 317 Ohms, reading again)
MAF 2.3 g/s
Injectors have been cleaned and rebuild and tested. I have a report showing results:
Inj # 1 170 CC/Min
InJ # 2 171 CC/Min
Inj # 3 170 CC/Min
Inj #4 160 CC/Min
SYS Balance 1.2 %
Total Sys LBS/Hr Static 64.76
CC fuel/Min H.P. Static 7.16
BSFC/ @ 80%/@EST. H.P. 0.55
Duty Cycle at Est. B.H.P. 0.73
@BSFC of .65 : 79.7
@BSFS of .55: 94.2
@BSFC of .50: 103.6
I will be changing the oil again for the 3rd time in case of fuel saturation and will be removing spark plugs for inspection as suggested and I will perform a block test for combustion gases.
As I mentioned before: I disconnected the vacuum hose from purge solenoid causing a vacuum leak and the HO2 sensor went to varing mv about 10mv to 900mv . The Injector pulse width drop to about 3 ms +or - Lean Rich status fluctuating between both.
My thoughts on this is that I created UN-metered ahead of the IAC and MAF sensor. Is it possible either the IAC is only opening 50% because when I pinched it it died and didn't go to 400 rpm and or a Bad MAF sensor( Poor quality)?
"I disconnected the vacuum hose from purge solenoid causing a vacuum leak and the HO2 sensor went to varing mv about 10mv to 900mv .
The Injector pulse width drop to about 3 ms +or - Lean Rich status fluctuating between both." a great test. so the air leak dropped it to 3mS.
proving the O2 wakes up and that ECU is setting rich condition, and is some input to ECU is wrong, and sure MAF is one, cause.
so adding un-metered air causes O2 to wake up.
I agree,.
check maf carefully, for correct voltage on output pin key on nostart, then idle and then gunned. and trick below ( a crude dyno)
you have 4speed A/T so use it as a dyno for maf readings,
use AT for load, (in drive, voltmeter to Maf output at idel
then hand brake on , choked wheels and foot on the brake pedal, (safe) now stop the throttle hard, 3 seconds max. see if you can get 3 volts or more.
same test as A/T stall test. the clutch will limit RPM to 1500 to 2000 RPM in gear. this puts a huge load no engine. for short time. (short time to not overheat clutch)
maybe the MAF is offset high?, a rare event, but anything is possible on hot wire MAF.
try to find tag on MAF that shows this 58B00 ( I ask this because clones do not have this number)
USA pn. 1992 to 98
13800-58B00
good luck to you !!!
http://www.fixkick.com